Allen Mogul Pony Pivot Repair: Difference between revisions

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File:CenterPlateCasting201.png|An un-machined casting, #201 "Center Plate", from Allen Models of Michigan.
File:CenterPlateCasting201.png|An un-machined casting, #201 "Center Plate", from Allen Models of Michigan.
File:CenterPlateCasting with ReplacementSteelComponents.jpg|A broken #201 casting next to new steel components to be used to fabricate replacement on Allen Mogul #486.  The pivot point is cut from 3/4 inch [[CRS]].  I used an abrasive chop saw to rough cut 0.6 inch length part.  Cut a 4 inch length of 2 inch by 1/8 inch HRS steel for the plate.
File:CenterPlateCasting with ReplacementSteelComponents.jpg|A broken #201 casting next to new steel components to be used to fabricate replacement on Allen Mogul #486.  The pivot point is cut from 3/4 inch [[CRS]].  I used an abrasive chop saw to rough cut 0.6 inch length part.  Cut a 4 inch length of 2 inch by 1/8 inch HRS steel for the plate.
File:MogulRepairPonyPivot3170.jpg|The 3/4 inch round stock is mounted in the three jaw chuck.  It is faced and a 1/32 inch chamber is cut around the edge.  The part is not faced all the way to the center, as it will be drilled out.  This lessens the chance of damaging the cutting tool.
File:MogulRepairPonyPivot3170.jpg|The 3/4 inch round stock is mounted in the three jaw chuck.  It is faced at 400RPM and a 1/32 inch chamber is cut around the edge.  The part is not faced all the way to the center, as it will be drilled out.  This lessens the chance of damaging the cutting tool.
File:MogulPonyPivotRepair 3171.JPG|The 3/4 inch part is turned around in the three jaw chuck in order to turn the opposite face. The part is turned to 0.5 inches long. A center point is drilled in the part with a #4 HRS center drill
File:MogulPonyPivotRepair 3171.JPG|The 3/4 inch part is turned around in the three jaw chuck in order to turn the opposite face. The part is turned to 0.5 inches long. A center point is drilled in the part with a #4 HRS center drill
File:MogulPonyPivotRepair 3174.JPG|The hole is drilled through with a #10 drill.
File:MogulPonyPivotRepair 3174.JPG|The hole is drilled through with a #10 drill.
File:MogulRepairPonyPivot3175.jpg|The three phase power is turned off to the lathe, the head is disengaged, and the part is threaded to 1/4-20 by manually turning the three jaw chuck. The tap is held in the tailstock.  I like to lock the tailstock and gently feed the tap into the part until the threads are well established (about 2 or three turns).  Then I losen the tail stock and let the the part "pull in" in the tap the rest of the way.  The threads are cut all the way through the 1/2 inch long part.
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Revision as of 23:39, 12 October 2013


by Daris A. Nevil

I heard stories about how much maintenance goes into a live steam locomotive. Now that I'm an owner I am finding that I have to do some kind of repair or maintenance following almost every run. Most of what I have done has been to improve operation or change operation to my preference. But #486 experienced some real damage on a run at the Annetta Valley & Western Railroad during a recent run.

The Incident

A cool front blew through north Texas August 17, 2013. It was the first break in the heat all summer, so I took advantage of the opportunity. I made the first run on the track that morning. Unfortunately, the track had not been "walked", and as #486 began its climb out of Stamey Loop I noticed a 1/2 inch stick across the rails. I didn't have time to stop, and hoped the cow-catcher would throw the stick clearn of the tracks. Well, it didn't, and old #486 went right over it. The pony truck went right over it, followed by all six drivers. They didn't event derail! But the tender did, so I stopped to clear the track and re-rail. All seemed find, but I found that the pony truck kept derailing in curves. Another engineer passing by pointed out that #486's pony truck was not tracking straight. I got down on my hands and knees and noticed the pony truck pivot pin was missing.

By this time I was far from the engine stands. The same helpful engineer suggested I run backwards back to Terry Town Station. That worked like a charm, and I didn't derail anymore.

Upon closer inspection I realized that not only was the pivot pin missing, but the pivot bearing had broken off.

The OEM part that had broken was Allen Models #201, "Center Plate". It is a cast aluminum cover for the bottom of the saddle. The casting includes a pivot point for the pony truck. This cylindrical pivot is what broke completely off during the impact with the branch.

The Repair

I decided to manufacture my own "Center Plate" from steel components, mainly because I did not want to wait for a replacement part. I also wanted a stronger material than cast aluminum. I also decided to reduce the diameter of the pivot so the pony truck would have more vertical freedom.

The photos below show how I made the replacement parts.